Guys I built this 1441 for a buddy of mine, everything went real smooth, the engine runs great, and he has put about 1000 miles on it. We finally went to dyno it and it made no freakin power..... 186hp/103tq....AFR was around 12.9-13.0 across the board.
The build is a Gen II engine, Gen 1 cylinder (3mm), decked .003":
JE 13.5-1 3mm pistons
Williford ported head w/gen 1 valves and 65# springs, deck surfaced
Cams are 415/395 webs@106/108*
APE studs, cometic head gasket, stock base gasket
The compression test(cold, WOT, 2 diff gauges) AND LEAK DOWN w/ a cheap tester. The leak down was at least 2-3 mins on each cyl and numbers were steady and holding.
#1--180, 5%..... WD40 shot in the cyl and retested == 220psi (<---potential problem cylinder)
#2--200, 7%..... WD40 shot in the cyl and retested == 212psi
#3--200, 9%..... WD40 shot in the cyl and retested == 210psi
#4--205, 9%......WD40 shot in the cyl and retested == 217psi
From what I could tell, the slight amount of leakage sounded like it was coming up through the intake valves...we could hear a slight "fizzing" as the air was bubbling up past the seats. Nothing detectable from the exhaust or crank case.
So...obviously the cranking PSI is WAY off and I am sure that is where the missing HP is at.....But why is the compression so low? Here is a pic of the shortblock before I put the head on it. The numbers written on the block are the deck height for both the intake/exh sides of the pistons and the numbers on the pistons are the ring gaps.
With no base gasket, the deck height was between .002-.004 on average...adding the .010 compressed height of a stock base gasket put it at ..012-.014 on average and that was not really even with the gasket fully compressed.
I was fully expecting cranking PSI to be 220-230 psi....maybe more... Ring orientation is correct, the letters on the rings are pointed up, gaps are staggered. I had spun the engine over many times with the head off watching the pistons travel in the bores, there was no rings folded or acting funny.......Everything seemed perfect....
I checked the valve lash again last night and all were still in spec, althought a few had tightened up a couple thou but still in spec so.....
I am lost on this one now so....any thoughts, suggestions or experience is appreciated...